Page 17 - Industrisal Technology EXTRA 3rd August 2020
P. 17

The bearing pairs on the third line were being
       overloaded. The premature bearing wear had
       allowed misalignment with the preceding and
       following lines. Subject to how long the unit was
       continuing to run, the case bores and – ultimately –
       the second line wheel and fourth line pinion shaft
       respectively were also destroyed.”

       Thrust overload
       On further analysis, the prime contributor to the
       failure was found to be thrust overload, which could
       be seen from the asymmetrical bearing inner race
       wear, (always in the same direction). This had also
       worn the respective bores.Baggaley explains the
       assessment: “The gear case was set up and clocked
       on the horizontal borer. This confirmed that the
       general accuracy of the gear case was good – parts
       of both the bore pair were unworn giving us the
       original centrelines. Accordingly, the line could be
       re-bored oversize with a counter bore added for a
       Top Hat flange.
         “The low speed shaft interface was also
       damaged internally where it grips the Input shaft –
       unusually, the pick-up was caused at original   As part of the test, paint and dispatch procedure,
       installation when the parts were mated. While   the internals were reset and gear contacts verified.
       many high value components had been essentially   The unit was spin tested with bearing temperatures
       written-off, we were keen to find out whether   monitored to ensure they plateau at an acceptable
       refurbishment was still practically and commercially   level. The lube system was also refurbished.  These
       viable.”                             particular units were upgraded. An additional large
         Dana’s servicing team undertook in-depth   area high efficiency filter together with a remotely
       investigation, resulting in a detailed report, with   monitored particulate sensor were added.  The unit
       fully-costed recommendations. Any damage that   was tested with a throw away filter element, which
       rendered parts unusable were illustrated and   was then replaced with new on completion ready for
       explained; reusable and replacement parts were   despatch.
       clearly identified, allowing for accurate rebuild costs   On completion of the project, Dana were able to
       to be quoted.  Any optional elements and additional   return the unit ready to fit, demonstrating that
       recommendations were made clear to the customer.    refurbishment can be possible, even for extensive
         The build and refurbishment – with new and   damage, and at less than half the cost of a new
       existing parts – was undertaken by the service   unit. With the choice between OEM gear parts or
       team. Bore liners were fitted prior to installing   reverse-engineered items, costs to the customer
       bearings and axial floats set, checked and recorded.   could be further reduced and lead-time cut

                           August 2020 • INDUSTRIAL TECHNOLOGY EXTRA! • p17
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