Page 3 - June 2022 Track N Times
P. 3

FEATURE STORY




         Generators:  A Lifeline for Ballast and Grade



         By Tyler Beebe, Manager Ballast and Grade


           Loram equipment needs two sources of mechanically driven power to be able to move: Electrical power and hy-
           draulic power. On mainline rail grinders, electricity is generated by main diesel engines attached to large genera-
           tors creating power for the grind system, computers, and traction (using an auxiliary generator for maintenance or
           back-up). On ballast and grade equipment (minus 2  generation SBC’s), electricity is supplied by a standalone die-
                                                         nd
           sel generator that powers the computers, HVAC, lights, air compressor, and PLC control systems. If the machine
           generator goes down, we are not able to travel or work the machine. It was common practice in the past to use
           the welder as a source of back-up power until the generator was repaired, but customers are pushing back on us-
           ing the welder as anything but a way to get off track should a generator go down. Now more than ever there is a
           high level of importance on keeping the machine diesel generators in top working order, as we work behind the
           scenes to build our spare inventory, until new tier 4 generators become available in 2023.

           This leads into a recent generator adventure on BC20 that shows the dedication, perseverance, and problem-
           solving ability of our field operations group to find solutions to complex problems. It all started when a phone call
           came in that the generator on BC20, an obscure 4.5L John Deere that is a one off in our fleet, began to have ex-
           cessive blow by, power loss, and intermittent shut down issues. We were able to find a technician from a John
           Deere Ag dealership to diagnose the problem as a failed turbo. We sourced a turbo and got it overnighted. After
           installing the turbo, the generator would still not run properly, now the diagnosis was that we needed a new en-
           gine  as  the  rings  and  bearings  were  gone  in  this  engine.  We
           searched for a replacement, everything was a week out at least,
           except for a local farmer who had three 4.5L diesels that he had
           used as irrigation pumps. We spoke with the farmer and were
           able to buy one of his engines. We found a local diesel mechanic,
           and work began to swap the blown-up engine for the used en-
           gine.

           It took one day to swap the engines out, integrate, and test. Mis-
           sion  success.  We  were  down  for  three  days  (1  day  for  when
           generator originally failed, one day for turbo swap and diagnosis,
           one day for farmers engine swap). Not bad considering the alter-
           natives and the unknowns going into the plan. The new engine
           worked great for about a week until disaster struck. The spare
           engine had a complete failure! We were back to square one. No
           spares, no available generators, and the farmer had sold his other
           two engines when word got out locally. The team regrouped and
           came up with a plan that could work; a rental generator until a
           permanent solution was found. We located a 20kW rental gen-

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