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Case 2                               Date: 14.05.2018                      Time: 11:00 hrs.



             Incident

            One  tower  mounted  remote  operated  HVLR  no.3
            testing  was  in  progress,  when  water  was  charged,
            suddenly  HVLR  motor  got  detached  from  it's
            original  position  &  fell  down  on  the  floor  from  the
            tower due to jerk. Immediately operation was stopped
            & area was barricaded.

















             Root Cause

           1.  Excessive vibration while operating the ROLRM.

            2.  Restriction in movement of Jet/Fog assembly of ROLRM-03 – As seen from the site snap of the jet / Fog
              nozzle,debris  particles  are  found  on  the  nozzle  outlet,  which  is  creating  restriction  in  movement  of
              Jet/Fog nozzle led to excessive load/pressure on motor as well as base frame of Jet/Fog Nozzle.


             Recommendations

           1. 1.  It is proposed to provide MOV operated HVs (in place of SOV) with bypass line for operating the all
              ROLRMs of PP Unit (4 Nos.) as its operation is very smooth because of its controlled opening. It has
              been verified with MOV operated ROLRMs of Swing Unit.

            2.  The debris materials observed at the nozzle to be cleaned periodically. The same to be included in the
              checklist of PM jobs.

            3.  Filter to be provided in the SOV/Pneumatic relay vent port to ensure proper operation of HVs.

            4.  ROLRM operation checking is to be done from its local start panel, not from SOV knob of HVs.























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